ANALYSIS OF FORCED OUTAGES -  STPS SARNI   2009-10
 
OCTOBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION PERIOD IN HR:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
1 UNIT-2 11.09.2009 04.10.2009 557.58 34.87 A.O.H.  
               
  FORCED
1 UNIT-1 04.10.2009 04.10.2009 0.37 0.04 TST Getting normal parameters, Unit synchronised.
07.10.2009 08.10.2009 4.27 0.28 TST MS TEMP LOW Getting normal parameters, Unit synchronised.
30.10.2009 31.10.2009 27.26 1.72 HT Incomer Breaker Flesh Over Fault attended & Unit Synchronised.
2 UNIT-2 04.10.2009 10.10.2009 135.16 8.45 Turbine control valve problem Fault attended & Unit Synchronised.
10.10.2009 17.10.2009 156.51 9.80 Turbine control valve problem Fault attended & Unit Synchronised.
3 UNIT-3 11.10.2009 11.10.2009 2.27 0.15 415 Volt Supply fail Fault attended & Unit Synchronised.
4 UNIT-4 15.10.2009 1710.2009 32.12 2.01 Boiler T/L Tube Leakage attended & Unit synch.
5 UNIT-5 NO TRIPPING
6 UNIT-6 21.10.2009 23.10.2009 47:25 9.48 Condenser Tube Leakage Tube Leakage attended & Unit synch.
7 UNIT-7 03.10.2009 03.10.2009 0:30 0.11 PRDS control v/v fail Fault attended & Unit Synchronised.
05.10.2009 07.07.2009 51:50 10.89 Reheater Tube Leakage Tube Leakage attended & Unit synch.
08.10.2009 08.10.2009 07:35 1.59 Air Heater 7B Outage Fault attended & Unit Synchronised.
26.10.2009 26.10.2009 09:55 2.08 Hotwell level control V/v MC fail Fault attended & Unit Synchronised.
7 UNIT-8 06.10.2009 06.10.2009 01:40 0.35 Furnace Draught High Getting normal parameters, Unit synchronised.
06.10.2009 06.10.2009 01:00 0.21 Furnace Draught High Getting normal parameters, Unit synchronised.
11.10.2009 12.10.2009 27:35 5.79 Condenser Vaccum problem Getting normal parameters, Unit synchronised.
13.10.2009 13.10.2009 02:50 0.60 PA fan 8B Temp. high Fault attended & Unit Synchronised.
8 UNIT-9 30.10.2009 01.11.2009 33:50 7.11 LTSH T/L Tube Leakage attended & Unit synch.
               
   
   
NOVEMBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION PERIOD IN HR:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
            NIL  
  FORCED
1 UNIT-1 27.11.2009 28.11.2009 20:49 1.30 Water Wall Tube Leakage Tube Leakage attended & Unit synch.
2 UNIT-2 05.11.2009 06.11.2009 35:37 2.23 Water Wall Tube Leakage Tube Leakage attended & Unit synch.
14.11.2009 14.11.2009 06:17 0.39 DMW Line leakage Fault attended & Unit Synchronised.
3 UNIT-3 05.11.2009 06.11.2009 36:53 2.31 Water Wall Tube Leakage Tube Leakage attended & Unit synch.
13.11.2009 14.11.2009 03:26 0.22 BFP Outage Fault attended & Unit Synchronised.
14.11.2009 14.11.2009 01:30 0.07 Low Vaccum Getting normal parameters, Unit synchronised.
4 UNIT-4 23.11.2009 26.11.2009 78:53 4.93 M.S. Temp. Low Getting normal parameters, Unit synchronised.
29.11.2009 30.11.2009 19:01 1.19 Primary S/H Tube Leakage Tube Leakage attended & Unit synch.
5 UNIT-5 12.11.2009 14.11.2009 43:39 2.73 Condenser Tube Leakage Tube Leakage attended & Unit synch.
21.11.2009 21.11.2009 03:15 0.20 Low Vaccum Getting normal parameters, Unit synchronised.
6 UNIT-6 NO  TRIPPING
7 UNIT-7 12.11.2009 12.11.2009 02:40 0.56 PA Fan 7B Lube Line Leakage Fault attended & Unit Synchronised.
13.11.2009 16.11.2009 77:35 16.29 LTSH Tube Leakage Tube Leakage attended & Unit synch.
8 UNIT-8 21.11.2009 21.11.2009 02:35 0.54 Turbine protection coil operated Fault attended & Unit Synchronised.
30.11.2009 30.11.2009 01:13 0.26 FSSS operated Getting normal parameters, Unit synchronised.
9 UNIT-9 01.11.2009 01.11.2009 08:20 1.75 LTSH Tube Leakage Tube Leakage attended & Unit synch.
12.11.2009 14.11.2009 39:10 8.23 Economiser Tube Leakage Tube Leakage attended & Unit synch.
15.11.2009 17.11.2009 49:10 10.29 LTSH Tube Leakage Tube Leakage attended & Unit synch.
DECEMBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION PERIOD IN HR:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
            NIL  
  FORCED
1 UNIT-1 22.12.2009 22.12.2009 00:34 0.04 TST Low Vaccum Getting normal parameters, Unit synchronised.
2 UNIT-2 17.12.2009 18.12.2009 20:12 1.26 TST Spray valve leakage Getting normal parameters, Unit synchronised.
22.12.2009 22.12.2009 02:16 0.14 TDT MS Temp drop Getting normal parameters, Unit synchronised.
3 UNIT-3 NO  TRIPPING
4 UNIT-4 07.12.2009 09.12.2009 41:17 2.58 PSH Tube Leakage Tube Leakage attended & Unit synch.
5 UNIT-5 05.12.2009 07.12.2009 47:24 2.96 PSH Tube Leakage Tube Leakage attended & Unit synch.
07.12.2009 08.12.2009 33:19 2.08 Water Wall Tube Leakage Tube Leakage attended & Unit synch.
6 UNIT-6 18.12.2009 19.12.2009 23:05 4.62 Non availability of coal,CHP problem Unit Synchronised after resuming Coal Supply
23.12.2009 23.12.2009 01:35 0.32 To attend R phase dropper of Generator bay No. 21 Fault attended & Unit Synchronised.
29.12.2009 30.12.2009 31:00 6.20 Economiser Tube Lealage Tube Leakage attended & Unit synch.
7 UNIT-7 NO  TRIPPING
8 UNIT-8 13.12.2009 15.12.2009 50:22 10.58 PA Fan 8B Outage Problem attended & Unit Synch.
17.12.2009 18.12.2009 37:15 7.82 Furnace protection Getting normal parameters, Unit synchronised.
21.12.2009 21.12.2009 01:33 0.33 Furnace protection Getting normal parameters, Unit synchronised.
21.12.2009 21.12.2009 01:15 0.26 Furnace protection Getting normal parameters, Unit synchronised.
23.12.2009 25.12.2009 33:55 7.12 Water Wall Tube Leakage Tube Leakage attended & Unit synch.
27.12.2009 28.12.2009 11:45 2.47 PA Fan 8B Outage Problem attended & Unit Synch.
9 UNIT-9 NO  TRIPPING