ANALYSIS OF FORCED OUTAGES -  ATPS CHACHAI   2009-10
JULY
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION OUTAGE IN  HOURS:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
3 UNIT-3     0.00 0.00    
4 UNIT-4 26.07.09   144:00 17.28 C.O.H. C.O.H.is being carried out.
  FORCED
3 UNIT-3 03.07.2009 09.07.2009 151:40 18.20 Tube leakage in Cage Bypass. Tube Leakage Attended.
21.07.2009 21.07.2009 6:08 0.74 Furnace Dark. After purging,unit restarted.
22.07.2009 27.07.2009 107:50 12.94 Tube leakage in Cage Bypass. Tube Leakage Attended.
27.07.2009       Generator Seal Face Temp. rise Unit is under shutdown.
4 UNIT-4 07.07.09 07.07.09 7:35 0.91 Electrical fault Fault Attended & Unit restarted
08.07.09 20.07.09 296:17 35.554 Tripped on Furnace Protection. After purging,unit restarted.
21.07.09 24.07.09 94:55 11.39 Furnace Dark, HR/CR line hangers got broken. Unit declared on C.O.H.w.e.f.25.07.09
  TOTAL     0.00 79.73    
 
AUGUST
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION OUTAGE IN  HOURS:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
3 UNIT-3     0.00 0.00    
4 UNIT-4     0.00 0.00    
  FORCED
3 UNIT-3 27.07.2009 06.08.09 248:35 29.83 Generator Seal Face Temp. rise Generator Seal replaced & Unit restarted
06.08.09 08.08.09 46:40 5.60 Relay oil pressure low  Unit restarted & synchronised.
11.08.09 13.08.09 25:40 3.08 Relay oil pressure low  Unit restarted & synchronised.
19.08.09 19.08.09 6:25 0.77 220 KV Station Supply Failure  Unit restarted & synchronised.
19.08.09 20.08.09 20:58 2.52 Low Farward relay operated  Unit restarted & synchronised.
20.08.09 20.08.09 1:25 0.17 Relay oil pressure low  Unit restarted & synchronised.
20.08.09 21.08.09 5:28 0.66 Relay oil pressure low  Unit restarted & synchronised.
21.08.09 23.08.09 59:10 7.10 Relay oil pressure low  Unit restarted & synchronised.
4 UNIT-4 25.07.09       C.O.H.  
  TOTAL       49.73    
SEPTEMBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION OUTAGE IN  HOURS:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
3 UNIT-3     0.00 0.00    
4 UNIT-4 25.07.09       C.O.H.  
  FORCED
3 UNIT-3   (120 MW) NO  TRIPPING
4 UNIT-4   (120 MW) 25.07.09       C.O.H.  
UNIT-5    (210 MW) 13.09.09 13.09.09 04:41 0.96 System Jerk Fault attended, Unit restarted & synchronised.
17.09.09 20.09.09 51:31 10.82 Station XR tripped on Earth Fault Fault attended, Unit restarted & synchronised.
22.09.09 22.09.09 03:26 0.72 Generator Protection Operated Fault attended, Unit restarted & synchronised.
  TOTAL     0.00 12.50