ANALYSIS OF FORCED OUTAGES -  ATPS CHACHAI   2009-10
OCTOBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION OUTAGE IN  HOURS:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
1 UNIT-3     0.00 0.00    
2 UNIT-4     744:00 89.28 C.O.H. C.O.H.is being carried out.
  FORCED
1 UNIT-3 07.10.2009 07.10.2009 8:58 1.08 Failure of 6.6 KV unit & Station Supply Supply restored & Unit Synchronised
2 UNIT-4 C.O.H.
3 UNIT-5 13.10.2009 13.10.2009 3:36 0.756 Tripped due to Drum Level protection auto control failed Unit restarted
  TOTAL     0.00 1.83    
 
NOVEMBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION OUTAGE IN  HOURS:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
1 UNIT-3     0.00 0.00    
2 UNIT-4     720.00 86.40 C.O.H. C.O.H.is being carried out.
  FORCED
1 UNIT-3 11.11.2009 13.11.2009 53:50 6.46 Boiler Tube Leakage Tube leakage attended,Unit synch.
2 UNIT-4 C.O.H.  
3 UNIT-5 01.11.2009 01.11.2009 11:50 2.485 Tripped due to PA Fan control damper malfunctioning Unit re-started & Synchronised.
  01.11.2009 01.11.2009 3:44 0.784 Both I.D.Fan tripped on over current. Unit re-started & Synchronised.
  TOTAL       9.73    
DECEMBER
S.N. DETAILS DATE OF SHUTDOWN DATE OF SYNCHRONISATION OUTAGE IN  HOURS:MIN MU  LOST REASON CORRECTIVE ACTION TAKEN
  PLANNED
1 UNIT-3     0.00 0.00    
2 UNIT-4     744:00 89.28 C.O.H. C.O.H.is being carried out.
  FORCED
1 UNIT-3   (120 MW) 16.12.2009 20.12.2009 105:30 12.66 Economiser tube leakage Tube leakage attended,Unit synch.
23.12.2009 26.12.2009 65:15 7.83 Pendent Reheater tube leakage Tube leakage attended,Unit synch.
2 UNIT-4   (120 MW)         C.O.H.  
3 UNIT-5    (210 MW) 09.12.2009 09.12.2009 02:47 0.59 PA fan IGV control failure Fault attended, Unit restarted & synchronised.
09.12.2009 10.12.2009 03:37 0.76 Drum Level very high Unit re-started & Synchronised.
10.12.2009 10.12.2009 10:21 2.17 Main Steam temperature Low Unit re-started & Synchronised.
10.12.2009 10.12.2009 3:30 0.74 Drum Level very high Unit re-started & Synchronised.
16.12.2009 18.12.2009 33:17 6.99 Generator Stator E/F relay operated Unit re-started & Synchronised.
  TOTAL     0.00 11.24